Quantcast
Jump to content


CapnWalleye

Members
  • Posts

    4
  • Joined

  • Last visited

Recent Profile Visitors

The recent visitors block is disabled and is not being shown to other users.

CapnWalleye's Achievements

Newbie

Newbie (1/14)

  • First Post
  • Week One Done
  • Conversation Starter

Recent Badges

0

Reputation

  1. Thanks. I tested compression which is over 100. Since my most recent post I've also looked at the fuel system and wondering if there's something that is affecting fuel flow. I pulled the lines and blew them out but could not find a filter. Also, I wonder if I made a mistake when adjusting the valves. Intake was tight but exhaust was still good. After doing it, though, I fear I didn't have it at TDC. I couldn't find the marks so spun it around to just after the exhaust opened and closed but before intake opened and closed. TDC is on the compression stroke if I remember correctly (I'm not a mechanic, just a guy who isn't afraid to get his hands dirty) which would be between intake opening but before exhaust, right?
  2. Thanks for this. I pulled the pump but cannot find a filter or screen. I didn't want to disassemble it without knowing more. I'll look at installing an inline filter ... good idea.
  3. Just picked up a Cub Cadet 500 that had shift issues (corroded fan gear) which I fixed. It also didn't seem to be running smoothly then all of a sudden it got worse. It seems to miss on both idle and when pushing the gas pedal to the floor and doesn't seem to be running at full power. I've been working with a local person who is walking me through some steps, but I'd like some input from this group as well. What I've done: - drained the fuel tank and replaced it with 93 octane fuel and added heet to help with any water problems. - replaced the fuel injector. - disconnected the battery (several times) to allow the module to reset. - set the valve clearance, both intake and exhaust, within specs ... intake was tight but exhaust seemed fine. - replaced the battery. - replaced the O2 sensor. Nothing has helped. Not sure what the next steps are, but would appreciate any expertise that can be offered here.
  4. Just picked up a Hisun 500 that had shift issues (corroded fan gear) which I fixed. It also didn't seem to be running smoothly then all of a sudden it got worse. It seems to miss on both idle and when pushing the gas pedal to the floor and doesn't seem to be running at full power. I've been working with a local person who is walking me through some steps, but I'd like some input from this group as well. What I've done: - drained the fuel tank and replaced it with 93 octane fuel and added heet to help with any water problems. - replaced the fuel injector. - disconnected the battery (several times) to allow the module to reset. - set the valve clearance, both intake and exhaust, within specs ... intake was tight but exhaust seemed fine. - replaced the battery. - replaced the O2 sensor. Nothing has helped. Not sure what the next steps are, but would appreciate any expertise that can be offered here.
×
×
  • Create New...